![Image](http://www.blackomega.com/boost.jpg)
1bar is normal but the flattening out in the middle is not.
Facts at hand:
* Turbo is a blitz K1-380V, boost curve when motor previously installed was fine
* Fuel pump was changed to Walbro 250LPH model while engine was out
* No boost controller installed, turbo VSV is disabled
* No obvious boost leaks
* Wastegate actuator is not obviously bent - first idea was that it might have got knocked at some stage so the wastegate is slightly open when it should be sealed - however it doesn't visually appear to be moved/damged
* With the actuator disconnected 1.3bar is easily obtained quickly and early in the rev range [this is when I took my foot off]
* Car boosts smoothly - no obvious bucking indicating ignition problems
Lastly, I'm going to try to pressure test the actuator tomorrow to make sure its not opening too early....
Any ideas greatly appreciated as this really has us stumped.....