i've a 3SGTE rev4 out of an Caldina ST215 running in my MR2 MK1.
(rebuilt engine, wiseco Pistons, 3" Exhaust, Haltech E8)
the last 2 years i drove with ~0,7bar (~10psi) - no Problem at all
last Friday my Haltech Tuner activatet the Haltech Boost Controll Solenoid.
(the port on the wastegate actuator which would normaly go to the vsv is blocked off, the line from the Turbo to the actuator is spliced and fitted both sides to the boost controll solenoid, the third port on the solenoid goes to free air)
with the boost controll solenoid activatet the boost goes on the dyno up to ~1,2bar (17psi) @4500rpm, then it drops to ~0,8bar (~11,5psi) and at ~6000rpm it rises slightly to ~0,9bar (~13psi)
on the road i have spikes of ~1,4bar (20psi) and then it drops to ~0,9bar (~13psi)
a can also hear a rattle noise wenn boost drops...
would a other wastegate actuator with a harder spring help here?
or what do you guys think is the problem???
this is the dyno sheet:
