Long story short.
Originally it took 30km before faltering occasionally then clearing, and she's all good.
After first two break downs with tows, two visits to the mechanic ($445) with assurances at each visit that the problem has been remedied.
The damn thing began stumbling again on Sunday after 7kms travel. We managed to reach our destination without coming to a complete stop ; a distance of 12km.
Looking back, this 7kms seems to be the common distance when the problem first shows, then gets worse till a full stop and no starting.
Anyhow, on our return 3 hours later it started up and ran fine until, sure enough at about 7kms it begins to stumble etc. We made it home.
Now here is the interesting bit. Sitting in the driveway we ran it up the rev scale and held it there until it began to miss(?) and run rough. I smelled something that seemed familiar so into my chair and to the exhaust end.
Sure smells like burnt fibreglass (?). I got my wife to drop the revs and I felt the pressure at the pipe- not too strong I thought. So she brought it up to higher revs and I couldn't detect any appreciable increase in flow but it was bloody hot and that strange stink.
Shut down the car and went inside.
The next morning it started fine with good exhaust pressure that increased with revs as you would expect. So we went for a test drive. This time we decided to drive 6 km and then return so that when it crapt out we would be able to get home. Sure enough, 10km later...................
I have had the exhaust system checked and it is all good (no cat either)
Items replaced by mechanic: fuel filter, distributor cap, rotor, electronic coil, plugs.
I called him and he said it had indicated a code 31 but he wasn't convinced that was the problem.(????)
Vacuum line to the MAP sensor appear /feel pliable and no sign of splitting. I disconnected the plug and closed up the female contacts then re-attached the connector; now nice and tight. It came off easier than when I attached it so could have been loose. Strange, the sensor(?) from the airfilter housing was disconnected)I wonder when that happened as it was in position when I fitted a good intake hose ( the other was completely split)
Its off to the local electrician for a plug-in today. Fingers crossed he gets a result and its not another exercise in cash for no remedy
Can anyone shed light on this problem? I am tired of throwing funds at it with no result.