Went to Manfeild yesterday, third run of the day and lost boost. Pulled into the pits checked hoses and all looked fine. Started car again then had white smoke (or water vapour) pouring out of the exhaust.
Trailered home.
Today I did a compression test and it is low in 3 & 4. It has always been a perfect 150psi on all but now 3 & 4 is down to 120. Lots of air coming out with the oil filler cap off. Interesting note, the wiring cover which runs across the end of the cam covers has melted!?
Took the turbo off and it has lots of play, this was a brand new Garrett item when put on and has done less than 10,000km and never over 13psi.
I have no idea what has happened to the turbo.
Compression is probably the head gasket but I suppose it could be the rings.
$$% sake this is going to expensive.
