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Take it the head has been machined and crack tested?ants_ae92 wrote: My ongoing problems with my 4age continue.
Blown headgasket - replaced
Blocked radiator - because of the blown radiator (flushed and cleaned)
If the system is still pressurising theres a good chance you still have combustion gases in the cooling system, get a tk or cyl leakage test done then go from there or you will be walking around in circles....ants_ae92 wrote: had/have a pressurised cooling system, which we thought the flushed radiator would have fixed.
ants_ae92 wrote:
My ongoing problems with my 4age continue.
Blown headgasket - replaced
Blocked radiator - because of the blown radiator (flushed and cleaned)
Take it the head has been machined and crack tested?
ants_ae92 wrote:ants_ae92 wrote:
My ongoing problems with my 4age continue.
Blown headgasket - replaced
Blocked radiator - because of the blown radiator (flushed and cleaned)
Take it the head has been machined and crack tested?
No the head had no signs of warpage at all, so we left it.
looks like I might just take it off the road, as I was going to do a turbo conversion with a small port motor/gze pistons. So I think I will just go the whole hog and do it properly with that motor. I dont want to have to spend money on a motor im just going to pull out and sit in the garage.
Thanks for your help man.
deaf_rattle wrote:
i didnt realise warping was visible
True-No-Turbo wrote:deaf_rattle wrote:
i didnt realise warping was visible
It isnt.
do it once do it right.
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True-No-Turbo wrote:
deaf_rattle wrote:
i didnt realise warping was visible
It isnt.
do it once do it right.
yes i realise that
and yes, do it once and do it right
deaf_rattle wrote:True-No-Turbo wrote:deaf_rattle wrote:
i didnt realise warping was visible
It isnt.
do it once do it right.
yes i realise that![]()
and yes, do it once and do it right
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